Today we spent all of Monday and most of Tuesday morning (6am) finishing up our robot.

  • New CIM motors (2)
  • New metal plating
  • New chain
  • Geared up 2:1
  • Trimmed the pvc
  • Mounted plastic on the side, back, and front ramp
  • Had to take it all apart to take off little pieces of covering…for 2 hours
  • Got the hood up and working
  • Made an extra roller
  • Polycord is done
  • Bumpers are on
  • Camera was mounted…but then the 5V channel on the Power Dist./ Board failed
  • Electrical is secure; resoldered again
  • Battery mount secured

The robot is up and running.  We had successful trials of testing on the field starting around 3 AM (our first run ever)

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Still got a ways to go…

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Our robot is ready for our first test run.